After a little bit of a break, I spent about ten minutes regaining my confidence in myself, and getting her fired up. A few small adjustments, and the hiccuping and fifty kick starts were history.
Much better than the over TWO WEEKS (spare time, der) I spent redoing all of my timing and jetting, pulling the carb, changing head gaskets, putting it all back together, checking the wiring and battery, only to find....nothing.
The problem? I was somewhat ridiculed for having .031" slow and .072" main jets in my Super B. Too much for a .020" overbored 74" Shovelhead.
Bullshit.
Next time, I will listen to myself. The original problem was that the slow jet was adjusted out farther than recommended, about 3½ turns..my first impulse was to go up to a .033", but the conversations went the other way. I still think I was right. And I still think I will.
Blue Bonnie and Clyde
Nice to enjoy the sunshine.
FTW, cogito ergo sum, bravo man.
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